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Precautionary landing goes bad

By NTSB · October 27, 2014 ·

Aircraft: Swift GC-1A. Injuries: 2 Fatal. Location: East Moriches, N.Y. Aircraft damage: Destroyed.

What reportedly happened: The airplane departed with an adequate supply of fuel in the main fuel tank but an unknown amount in the tip tanks. The Swift’s takeoff was witnessed by the mechanic who performed the last inspection on the airplane. The mechanic thought the engine sounded unusual and thought the pilot would return for landing, but he did not.

The airplane’s GPS indicated that the flight proceeded south to the southern Long Island coastline then turned to the west, paralleling the coastline while climbing to a maximum altitude of 2,602 feet. The flight continued on the westerly heading and descended to 2,383 feet and then turned north. The flight continued on the northerly heading and descended to 1,812 feet, then turned to an easterly heading, followed by a southeasterly heading then back to an easterly heading with a steadily decreasing altitude and a steady groundspeed of about 86 knots. When just west of Moriches Inlet, the GPS altitude was noted to be 60 feet, and the groundspeed was 85 knots.

Several witnesses near the crash site heard a sputtering engine. One witness stated that the airplane was running flawlessly, but he thought it was going to land because it was flying “way too slow.” Another witness who was about 1,000 to 1,500 feet west of the Moriches Inlet, reported seeing a flock of birds take flight followed by the airplane pitching up and then pitching down into the inlet.

Although minimal damage was noted on the propeller, no evidence of a bird strike was noted on any component of the airplane. The flaps and landing gear were extended, consistent with a precautionary landing.

The fuel selector was found positioned to the tip tanks, both of which were breached during the impact, therefore no determination could be made as to the quantity of fuel in the tanks at the time of the accident.

Although the remaining quantity of fuel in the main fuel tank was not quantified during the post-accident investigation, the airplane had only been operated for 40 minutes since the main fuel tank was filled and the main fuel tank can hold over two hours of fuel.

No obstructions of the fuel supply from the main or tip tanks were noted, and the engine-driven fuel pump tested satisfactorily.

Although about six ounces of water was drained from the main fuel tank, the water was consistent with ocean water and no other contaminants from the tank were noted. Water contamination was also noted from a sample of fuel and water drained from an open fuel supply line for the right tip tank, however, the right tip tank was breached and the water was likely from the ocean. No fuel or contamination was noted in the carburetor bowl.

Although a valve on the left side of the firewall was inoperative, which allowed heated air to enter the cockpit by the pilot’s side, no determination could be made as to how or if that factored into the accident sequence. Further, that condition had been known by the pilot since September.

Based on the flight track and groundspeed recorded by the GPS and the fact that the landing gear and flaps were extended, investigators determined that it is likely that the pilot was performing a precautionary landing. However, the reason for the attempted precautionary landing could not be determined from the available evidence. Based on the witness statement of birds in the area, it is likely that during the precautionary landing, the pilot reacted to the birds by pitching the airplane up, stalled the airplane, and was unable to recover because of the low altitude.

Probable cause: The failure of the pilot to maintain airspeed while attempting a precautionary landing for reasons that could not be determined from the available evidence. Contributing to the accident was the pilot’s pitch-up reaction to birds that took flight during his approach for the precautionary landing, which resulted in an inadvertent stall

NTSB Identification: ERA13FA032

This October 2012 accident report is are provided by the National Transportation Safety Board. Published as an educational tool, it is intended to help pilots learn from the misfortunes of others.

About NTSB

The National Transportation Safety Board is an independent federal agency charged by Congress with investigating every civil aviation accident in the United States and significant events in the other modes of transportation, including railroad, transit, highway, marine, pipeline, and commercial space. It determines the probable causes of accidents and issues safety recommendations aimed at preventing future occurrences.

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Comments

  1. Steve says

    October 31, 2014 at 8:20 pm

    Both occupants of the plane were friends of mine as well as the airport owner (Spadaro).

    From all indications, it seems like the engine probably displayed at least a minor amount of abnormality in its operation from the start, but the problem wasn’t perceived to be serious enough to turn back and land at Spadaro immediately. Republic isn’t that far away and I suspect that the pilot felt that he could make it back to home base without facing the inconvenience of being stranded at Spadaro.

    Apparently, the engine operation began to deteriorate and they decided to turn back. The decision to continue the flight or the late decision to turn back was the first “error”, but that was compounded by the flock of birds that got in the way causing a knee-jerk reaction to avoid them which sealed the fate of both occupants.

    Hopefully, those who are familiar with this event will have learned something from it.

  2. Jon says

    October 28, 2014 at 8:55 am

    I was flying about the same time and area this happened two years ago and had to make an emergency landing due to severe carb icing at climb power. The conditions were around 90% humidity and 50*F that morning. The engine started loosing RPM and I mentioned it to the owner of the airplane who has about 2K hours in make/model. He took over the controls and told me to declare an emergency while he maneuvered for landing. We were still in the pattern so were able to put it down on the runway and then off into the grass. When we got clearance to taxi back to the hangar we could develop full power. The owner was asked by the local group of pilots hanging out if he applied carb heat, (of which we did not,) but soon admitted that carb icing was the cause.

    A few days later I called the FAA to mention this story to help with the investigation when we heard of the Swift going down, the guy at the Farmingdale FSDO said he would note the conditions in the report. Looks like the NTSB didn’t think carb icing was a factor on this…….

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