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Fuel contamination leads to gear-up landing

By NTSB · May 28, 2018 ·

The pilot was taking off in the Mooney M20 when the engine began to sputter and lose power.

He elected to reduce engine power and land on the remaining runway at the airport in Little Rock, Arkansas, however he had already retracted the landing gear.

He lowered the landing gear handle, but was not able to lock the gear into place before the airplane hit the runway and the nose gear collapsed.

Post-accident examination of the airplane found water in the left and right wing fuel tanks, as well as the engine’s carburetor.

It is likely that the loss of engine power was a result of the water contamination of the fuel system.

Probable cause: A loss of engine power due to water contamination of the fuel.

NTSB Identification: CEN16LA200

This May 2016 accident report is provided by the National Transportation Safety Board. Published as an educational tool, it is intended to help pilots learn from the misfortunes of others.

About NTSB

The National Transportation Safety Board is an independent federal agency charged by Congress with investigating every civil aviation accident in the United States and significant events in the other modes of transportation, including railroad, transit, highway, marine, pipeline, and commercial space. It determines the probable causes of accidents and issues safety recommendations aimed at preventing future occurrences.

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Comments

  1. Jon says

    May 30, 2018 at 4:54 am

    Positive rate, NEGATIVE RUNWAY, gear up.

  2. JimH in CA says

    May 29, 2018 at 7:18 am

    Unfortunately, the NTSB report makes no mention of any pre-flight inspections that the pilot made.

    • Jon says

      May 30, 2018 at 4:54 am

      Yeah, I’d like to think that he should have noticed water in the fuel tester.

    • Joe Kohan says

      June 13, 2018 at 8:19 am

      If the pilot had conducted a true pre flight inspection, this incident could probably been avoided.

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