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Preliminary report on B-17 crash released

By General Aviation News Staff · October 16, 2019 ·

The NTSB has released its preliminary report on the Oct. 2, 2019, crash of the Collings Foundation’s B-17 Nine-O-Nine.

The plane crashed shortly after departure from Bradley International Airport (KBDL) in Windsor Locks, Connecticut, resulting in seven fatalities, five people seriously injured, and two with minor injuries.

Among those killed in the crash were pilot Ernest McCauley and copilot Michael Foster, along with five passengers. The flight mechanic/loadmaster and four passengers were seriously injured, while one passenger and one person on the ground suffered minor injuries.

The commercial sightseeing flight was conducted under the provisions of a Living History Flight Experience exemption granted by the FAA.

According to the preliminary report, visual meteorological conditions prevailed in the area and no flight plan was filed for the flight, which departed KBDL at 9:47 a.m.

The Collings Foundation’s B-17 “Nine-O-Nine”

According to preliminary air traffic control (ATC) data provided by the FAA, shortly after takeoff, at 9:50 a.m., one of the pilots reported to ATC that he wanted to return to the airport. At that time, the airplane was about 500′ above ground level (agl) on the right crosswind leg of the airport traffic pattern for Runway 6.

The approach controller verified the request and asked if the pilot required any assistance, to which he replied no. The controller then asked for the reason for the return to the airport, and the pilot replied that the airplane had a “rough mag” on the No. 4 engine.

The controller then instructed the pilot to fly a right downwind leg for Runway 6 and confirmed that the flight needed an immediate landing. He subsequently cancelled the approach of another airplane and advised the pilot to proceed however necessary to Runway 6. The approach controller also instructed the pilot to contact the tower controller, which he did.

The tower controller reported that the wind was calm and cleared the flight to land on Runway 6. The pilot acknowledged the landing clearance. At that time, the airplane was about 300′ agl on a midfield right downwind leg for Runway 6. The tower controller asked about the airplane’s progress to the runway and the pilot replied that they were “getting there” and on the right downwind leg. No further communications were received from the airplane.

Witness statements and airport surveillance video confirmed that the airplane struck approach lights about 1,000′ before the runway, then hit the ground about 500′ prior to the runway.

It then veered right off the runway before colliding with vehicles and a deicing fluid tank about 1,100′ right of the center of the runway threshold.

The wreckage came to rest upright and the majority of the cabin, cockpit, and right wing were consumed by fire.

The landing gear was extended and measurement of the left and right wing flap jackscrews corresponded to a flaps retracted setting. The flap remained attached to the right wing and the aileron was consumed by fire. The flap and aileron remained attached to the left wing and a section of flap was consumed by fire. The empennage, elevator, and rudder remained intact.

Control continuity was confirmed from the elevator, rudder, elevator trim, and rudder trim from each respective control surface to the area in the cabin consumed by fire, and then forward to the cockpit controls.

Elevator trim and rudder trim cables were pulled during impact and their preimpact position on their respective drum at the control surfaces could not be determined.

The left wing aileron trim tab remained intact and its pushrod was connected but bent. The left aileron bellcrank separated from the wing, but the aileron cables remained attached to it and the aileron cable remained attached in cockpit.

The Nos. 1 and 2 engines remained partially attached to the left wing and all three propeller blades remained attached to each engine. One propeller blade attached to engine No. 1 exhibited an 8″ tip separation. The separated section traveled about 700′ before coming to rest near an airport building.

Another propeller blade on the No. 1 engine exhibited chordwise scratching and leading edge gouging. The third propeller blade was bent aft.

The No. 2 engine propeller blades exhibited leading edge gouges and chordwise scratches.

The No. 3 engine was recovered from the top of the deicing tank. One blade was impact damaged and near the feather position. The other two blades appeared in a position between low pitch and feather. One propeller blade exhibited a 5″ tip separation and the separated tip sections were recovered from 100′ and 700′ from the main wreckage.

The No. 4 engine was recovered from the deice building. All three propeller blades on the No. 4 engine appeared in the feather position.

A fuel sample was able to be recovered from one of the No 3. engine’s two fuel tanks. The recovered sample had a visual appearance and smell consistent with 100LL aviation fuel and was absent of debris or water contamination. Following the accident, the fuel truck used to service the airplane was quarantined and subsequent testing revealed no anomalies of the truck’s equipment or fuel supply. Additionally, none of the airplanes serviced with fuel from the truck before or after the accident airplane, including another airplane operated by the Collings Foundation, reported any anomalies.

The airplane was manufactured in 1944, issued a limited airworthiness certificate in 1994, and equipped with passenger seats in 1995. It was powered by four Wright R-1820-97, 1,200-horsepower engines, each equipped with a three-blade, constant-speed Hamilton Standard propeller.

The airplane was maintained under an airworthiness inspection program, which incorporated an annual inspection, and 25-hour, 50-hour, 75-hour, and 100-hour progressive inspections.

Review of maintenance records revealed that the airplane’s most recent annual inspection was completed on Jan. 16, 2019. At that time, the airframe had accumulated about 11,120 total hours of operation.

Engine Nos. 1, 2, and 3 had 0 hours since major overhaul at that time. Engine No. 4 had 838.2 hours since major overhaul at that time.

The airplane’s most recent progressive inspection, which was the 100-hour inspection, was completed on Sept. 23, 2019. At that time, the airplane had been operated about 268 hours since the annual inspection.

NTSB officials note that this preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. It usually takes NTSB officials about 18 months to issue a final report.

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Comments

  1. Jaap du Preez says

    October 20, 2019 at 11:40 pm

    All fields with asterix * were filled ?

  2. Jaap du Preez says

    October 20, 2019 at 11:39 pm

    This “initial” report unfortunately indicates a possible pilot error.
    A left hand circuit would have been a better option keeping lazy wing high (dead donkey no 4)
    Such a tragic preventable loss
    RIP and condolences to friends & families

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