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Simulated engine-out approach goes wrong

By NTSB · December 28, 2020 ·

The pilot reported that, after he completed an aerial observation flight, he decided to conduct a simulated engine-out approach to an open field near Elk, California.

When the Cessna 175 was about 40 feet above ground level, he aborted the approach by applying full engine power and elevator back pressure. The descent was not immediately arrested, but the airplane seemed to be accelerating.

As the airplane continued to descend, it slipped left, and the left main landing gear hit a bush, which induced more left yaw and loss of lift.

Subsequently, the wing hit vegetation and terrain, and the airplane then cartwheeled and came to rest upright.

The airplane sustained substantial damage to the wings and fuselage.

The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause: The pilot’s failure to arrest the descent rate during an aborted simulated engine-out approach, which resulted in impact with vegetation and a subsequent cartwheel.

NTSB Identification: WPR20CA055

This December 2019 accident report is provided by the National Transportation Safety Board. Published as an educational tool, it is intended to help pilots learn from the misfortunes of others.

About NTSB

The National Transportation Safety Board is an independent federal agency charged by Congress with investigating every civil aviation accident in the United States and significant events in the other modes of transportation, including railroad, transit, highway, marine, pipeline, and commercial space. It determines the probable causes of accidents and issues safety recommendations aimed at preventing future occurrences.

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Comments

  1. Warren Webb Jr says

    December 29, 2020 at 8:39 am

    The pilot’s report stated he initiated the engine out glide at 65 kts with 30 degrees flaps but he didn’t state the airspeed at the attempted recovery point. Normally this model would be at about 65 kts and start the flare even lower and have a safe landing. Failure to arrest the descent suggests that airspeed had deteriorated by the time he reached 40′ agl and the back pressure stalled the wing.

  2. gbigs says

    December 29, 2020 at 7:07 am

    A 2500lb max gross plane with a 175hp engine that cruises at just above light sport speeds cannot be expected to reverse a descent at 40 feet with the engine at idle. This accident proves it.

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