• Skip to primary navigation
  • Skip to main content
General Aviation News

General Aviation News

Because flying is cool

  • Pictures of the Day
    • Submit Picture of the Day
  • Stories
    • News
    • Features
    • Opinion
    • Products
    • NTSB Accidents
    • ASRS Reports
  • Comments
  • Classifieds
    • Place Classified Ad
  • Events
  • Print Archives
  • Subscribe
  • Show Search
Hide Search

NTSB Accidents

Pilot loses control when landing gear fractures

By NTSB · May 15, 2024 ·

The pilot’s failure to maintain directional control during a touch-and-go landing after applying power for takeoff, which resulted in a runway excursion and noseover.

Sagging avionics trays contribute to Cessna 414 accident

By NTSB · May 13, 2024 ·

The pilot/mechanic’s failure to properly secure two airplane avionics units, which resulted in the trays supporting the units to sag downward and become lodged in the movement area of the elevator bellcrank during the accident takeoff.

Heart problems lead to fatal crash into the ocean

By NTSB · May 10, 2024 ·

A loss of airplane control due to pilot incapacitation, which resulted in an overflight of his destination and subsequent descent into water.

Obstructed vent outlets lead to fuel starvation

By NTSB · May 8, 2024 ·

A total loss of engine power during cruise flight due to fuel starvation resulting from obstructed forward and aft vent outlets in the left fuel tank.

Hole in brake line leads to accident

By NTSB · May 6, 2024 ·

Inadequate maintenance of the airplane’s brake system that resulted in a hole in the brake line, the loss of brake fluid, and the subsequent loss of brake functionality.

Improper leaning of engine proves fatal for two

By NTSB · May 3, 2024 ·

The pilot’s improper leaning of the engine during an extended period of time, which caused an exhaust valve to become stuck and led to the partial loss of engine power during the accident flight. Contributing to the accident was the pilot’s decision to attempt a second takeoff without having the engine further examined.

Improper maintenance leads to bent 172

By NTSB · May 1, 2024 ·

Loss of engine power due to the throttle linkage becoming disconnected in flight due to improper maintenance.

Missing hardware contributes to loss of control on landing

By NTSB · April 29, 2024 ·

The loss of directional control during the landing roll, due to missing hardware which resulted in the separation of the nose landing gear torque links.

Three injured when pilot loses control while landing

By NTSB · April 26, 2024 ·

The pilot’s failure to maintain directional control during landing, which resulted in a runway excursion.

  • « Go to Previous Page
  • Page 1
  • Interim pages omitted …
  • Page 44
  • Page 45
  • Page 46
  • Page 47
  • Page 48
  • Interim pages omitted …
  • Page 450
  • Go to Next Page »

© 2026 Flyer Media, Inc. All rights reserved. Privacy Policy.

  • About
  • Advertise
  • Comment Policy
  • Submit Press Release
  • Contact Us
  • Privacy Policy
  • Writer’s Guidelines
  • Photographer’s Guidelines